Nicholas Fluhart

April 3, 2012

Foreman Upgrades & Repairs Part 1: Brakes & Tie Rods

Filed under: Project: 475 Foreman — Nicholas Fluhart @ 6:11 pm

As I wrote here, few projects are ever really completed, and I’ve performed many upgrades to my 1998 Honda Foreman since I built it five years ago, so I thought I’d write a few posts to outline what I’ve done. I’ll start with the repairs I did after the 1st annual East Camden Expedition. As you can see there, I broke a tie rod end. Typically a tie rod will develop slack to let you know it is worn out, but this one gave no warning; it just flew apart. This was essentially the first time I had to lay a wrench on this ATV since I built it. So once I rolled it up in the shop I tilted it up onto the rear rack as seen below. This allows me to work on the front end while standing.

I removed the tie rod end from the steering knuckle, marked the threads on the tie rod, and removed the end. The aluminum ends are bad about seizing on the steel rods, so I painted the threads with anti-seize compound and installed the new end…then repeated the process on the other side. The inner ends were still in good shape, so I’ll squeeze more life out of those for now.

Applying Anti-Seize to Tie Rod

New Tie Rod Ends

So while I’m at it, I figured it would be a good time to go ahead and overhaul the front brakes. The brakes still had a good handle (like having a good pedal), but it wouldn’t actually stop. This is an indication that the drums are rough and without a good, smooth surface the shoes will not have enough to grab. That’s what my problem was here. I pulled the drums to inspect everything. The good news is that everything was still sealing good, so there was no mud. However, due to age I had one frozen wheel cylinder and a few adjusters as well. So I ordered new drums as seen below, and I went ahead and ordered all new wheel cylinders.

New Brake Drum Next to Old One.

Once my tie rods and brakes were squared away, I put the ATV back on the ground and proceeded to set the toe of the front wheels. The easiest way to accomplish this is to place the ATV on level ground and fasten the handlebars perfectly straight. You’ll see in the photo below that I use tie straps to hold the handlebars straight.

Then it’s just a matter of measuring and adjusting. First measure across the rear of the tires, center of one tire to center of the other, and note the distance. Then measure across the front of the tires, center to center. If the front measurement is greater than the rear, it’s toed out. If the rear is greater, it’s toed in. Some ATV’s require a certain amount of positive or negative toe, and some require it to be equal with no positive or negative toe. I don’t recall off hand what the Foreman required, but I set it appropriately and tightened the lock nuts on the tie rod ends and called it finished. It drives great, and with the new brake job, it threw me over the handlebars the first time I hit the brakes. That’s exactly what I wanted!

Stay tuned for the next round of repairs…

March 26, 2012

Retreiving Ditch Witch R40

Filed under: Project: Ditch Witch,Trucks & Equipment — Nicholas Fluhart @ 8:52 pm

Recently my buddy Philip called and told me he had acquired an old Ditch Witch, and knowing my love for old iron and that I have a similar Ditch Witch, he thought I might come out and help him haul it home. It’s a 1970’s vintage R40 in surprisingly good condition considering it hasn’t run for a few years. I hooked a trailer to my truck and since the machine was close to his house, Philip drove his dad’s new John Deere tractor over to assist with loading.

This R40 is equipped with a rear trencher and a 4-way push blade for back filling. After reviewing the situation, we knew the first order of business was to raise the blade and trencher so we could tow the machine out to the gravel road for loading as the ground was much too soft to back the truck and trailer up to the machine where it sat. We disconnected the hydraulic line to the lift cylinder on the blade and used a come-along to winch it up.

Once the blade was up, we moved back to the trencher. The hydraulic line to the lift cylinder on the trencher had a quick-connect coupler, so it was easy to disconnect the line. I used the front-end loader on the tractor to raise the trencher while Philip held the fitting open so the hydraulic pressure could release. Once raised, we chained it up to the roll bar. Then we hitched the machine to the tractor and Philip towed it onto the road while I steered.

I then positioned my truck so we could load it up. Again, using the tractor, Philip pushed while I steered it up onto the trailer.

The trailer had a long tail on it, and given the weight of the machine when coming up the ramps, it provided enough leverage to raise the rear of my half-ton truck. Subsequently, the brake on the truck was of no affect and the truck skid a few feet as seen below.

Once secured, I set out on the road with the machine in tow. It was a weighty load for my small truck, but it handled the load just fine. Once we arrived at our destination, Philip used the tractor to pull the Ditch Witch off of the trailer as I steered.

We looked the machine over. First, I checked the normal wear points, such as any pivot pins, sprockets, teeth, etc., and overall, it is very straight and tight. It shows to have fewer than 2k hours, and the hour meter is functional. This seems to support my conclusions on the overall condition. In fact, the only wear I could really find on the machine was the tires, one of which is coming apart. The previous owner indicated that there was a drive problem, which is probably why it hasn’t been used in five or more years. We located a broken drive chain from the transmission to the drive components and rear hydraulic pump. That’s likely to be our drive problem and should be a fairly easy fix given there is nothing more serious that caused the chain to break. We then attempted to run the engine. We did actually get it to fire a few rounds, but only on two cylinders. The engine is the classic Wisconsin four-cylinder air cooled unit. Having set out in the weather for half a decade allowed for some moisture to get into the two rear cylinders and seize the valves. This should also be a relatively easy fix as long as the cylinders are in decent shape. Philip has already begun work on this his first equipment project.

I believe this machine would be a handy addition to a good equipment collection, or a start to one. Typically, you can rent a trencher cheaper than you can own one, but when the price is a bargain, like this one and like mine, it’s a good unit to have. The R40 is a sizable machine, about twice a big as my 2300. It has enough weight to easily handle the trencher, blade, and then some. It has provision on the front for a backhoe attachment, which includes the mounting points and the hydraulic hookups. The machine has hydraulic pump driven off the engine crankshaft, and it has a hydraulic motor on the transfer case that actually drive the wheels when the machine is in trencher mode. I think this is going to be a fun project and a fun machine for him.

Until next time…

UPDATE: See the project post for this machine here.

March 23, 2012

2nd Annual East Camden AR Expedition: Day 3

Filed under: Trips and Fun — Nicholas Fluhart @ 9:34 am

Before posting the 2012 Expedition footage, I’m posting the final 2011 photos of the Day-3 Freestyle ride. I finally found these, and they’re pretty good…better than I remember.

So on Day-3, things really got crazy on the trails. Everyone knew it was our last ride before departing for home that evening, so it was wide open balls to the wall! Some had to cut out early, the rest of us stayed to have every last bit of available fun before heading back to civilization. Amazingly there were no casualties, aside from me taking a roll in the creek and Chris having to be towed back to camp after floating his machine. It’s all documented in the slideshow at the bottom of this post.

Here are some screen caps from the slideshow posted below:

The Foremans

Foreman Wheelie

I’ll soon be posting the 3rd Annual Expedition from 2012…

January 29, 2012

Mt. Holly January 2012

Filed under: Trips and Fun — Nicholas Fluhart @ 6:17 pm

Our annual Mt. Holly hunting trip, usually taking place in late October or early November, was postponed this last year due to excessive drought and fire bans. We reconvened the weekend of January 14th. We camped three nights and had a lot of fun. As always, there was plenty of food, guns, and riding to be had. Here are some of the few photos I have of the event:

It seems I have more pics of us cutting fire wood than anything else, nonetheless it was needed to survive the 20° nights and cold wind…

With camp provisions squared away, we set out for a hunt with the dog…

The next day it was too windy to hunt, so we engaged in some recreational shooting activities…

Our last night we had a pretty good ride, but after getting lost miles from civilization with temperatures rapidly dropping, no one was in the mood to take pictures.  However, after happening upon a rather oddly shaped tree, I couldn’t resist fishing out my camera and taking a few shots.

That wraps it up. Until next time…

December 25, 2011

Allis-Chalmers Forklift Cylinder Repair

Filed under: Project: AC Forklift,Trucks & Equipment — Nicholas Fluhart @ 5:30 pm

Well, after 30 years of service, age and wear had finally gotten to the hydraulic cylinders on my old Allis lift. You may remember previously I rebuilt the short lift cylinder and one tilt cylinder on the mast. Later, the long lift cylinder and the other tilt cylinder both began hemorrhaging. Bad became worse and soon I was loosing a gallon of fluid at every use. Fortunately, I had recently acquired a little Clark lift which took up most forklift duties around the complex. This bought me a little time for the repairs.

After the local hydraulic shop, in a state of incompetence, screwed up my short lift cylinder, I decided to rebuild this one myself. Rebuilding the long cylinder is no easy task for two reasons. One: Due to its location within the mast (not to mention its weight), it is heck to remove and reinstall. Two: It is also more complex than the short lift cylinder as the long cylinder has a feed tube with all the associated bushings and seals. At first glance, there’s no logical strategy for getting it out, and since my service manuals don’t cover anything to do with the mast, I’m flying purely on what I hope to be at least a moderate level of competence in terms of my skill level. Nevertheless, I endeavored to persevere.

Since I figured the mast would have to be raised at some point during the procedure, I had to work on it outside the shop. I began by removing the hydraulic line attached to the feed tube. Then I removed the nut that fixes the feed tube to the top stage of the mast. You’ll note that I’m using a manual ratchet instead of an air wrench on this because the nut is self locking, and often times if an air wrench is used, it will destroy the threads because of the high rate of speed.

Hydraulic Line Removed from Feed Tube

Removing Feed Tube Nut

Might I add, the humidity level that day, and throughout most of the project, had to have been 200% if that’s even possible, which explains the somewhat foggy photos and my drenched shirts. Moving on… Next, and before loosening anything else fixture-wise, I decided to loosen the gland nut while the cylinder was still firmly in place. I didn’t have a wrench big enough, so the next day I borrowed a large chain wrench which did the job nicely.

Feed Tube Nut

Loosening Gland Nut

Next, I had to raise the mast so I could lower the junction block at the top of the feed tube through the second stage of the mast. For this I took my Clark lift and raised the carriage on the Allis lift until the second stage of the mast begun to raise. This was NO easy task. The Clark lift would barely handle the weight. To make matters worse, the junction block is slightly offset and refused to go down through the hole in the second stage. Careful not to bend the feed tube, I pried and hammered a bit before logic struck at which time I decided to loosen the bottom mounting nut on the cylinder (exactly like the top nut on the feed tube). This allowed some wiggle room, and alas, it dropped through and the top of the cylinder was now completely free.

Feed Tube Junction Block

Raising the Mast

The next step in removing the cylinder was to finish the bottom mount and unhook the bottom hydraulic line, but first I made certain the mast was safely suspended. Don’t let the compact size of this machine and these parts fool you; this stuff is very heavy. The machine weighs about 13,000 lbs, and the mast components are made from very thick and very heavy steel. There is literally a ton of weight hanging above me here, so safety is very important. I used a strong, heavy-gauge pipe to hold the mast up, then I chained the top portion of the mast for a backup safety mechanism. I also had the carriage double chained.

Safety Check

When attempting to unhook the hydraulic line from the base of the cylinder, it became evident that there was not enough room to maneuver the wrench in the tight space. So I decided to unhook the line back at the hydraulic valve. This would give me slack enough so when I removed the cylinder I could pull the base out far enough to use the wrench to remove the line from the base of the cylinder. Back at the valve, I also had to unhook and move the hydraulic filter to have enough room to work at the valve.

Filter Moved Back from the Valve

Disconnecting the Bottom Hydraulic Line

Finally, the heavy cylinder was ready to come out.

Now that the cylinder is removed, it is time to disassemble the components for inspection at which time we can also take measurements which will be needed to order the new parts. We place the cylinder down where we can easily work on it and remove the main gland nut, and then the main ram easily pulls out of the bore. Then, using the same chain wrench, we remove the feed tube gland from the ram, and the feed tube pulls out. Then, although it’s not pictured, we removed the feed tube gland which proved to be extremely stubborn to slide off the tube, but a long pipe and a sledge hammer did the trick.

Loosening Feed Tube Gland

Removing Feed Tube from Ram

Once everything is apart I can begin measuring the components to place an order for new packing. I couldn’t simply measure the old seals because they had completely disintegrated. This explains the hemorrhaging, and it also explains how rainwater was entering the hydraulic system. Nevertheless, I took measure and proceeded into the office to do what the incompetent local hydraulic shop said was impossible: find new seals. After approximately one Google search and three minutes of viewing an online catalog, I easily found the parts I needed and placed the order. Since my application has a feed tube involved, it required the most expensive packing kit. This is largely due to the addition of bronze bushings and extra seals. However, it was still much cheaper than anything the local guys could have ever came up with and I was happy to find the parts. Now, on to the business of reassembling the cylinder…

First we took the feed tube gland and knocked out the old plastic bushings and replaced them with the new bronze bushings that came in the kit. We used the hydraulic press to install the new bushings:

Installing Bronze Bushings

Reinstalling the gland back on the feed tube proved almost as difficult as removing it. We used a brake cylinder hone to reach precisely the correct inside diameter of the bronze bushings, then we used a buffing wheel on a Dremel tool to polish off any scars on the chrome feed tube. After that, we were able to slide the gland back on the tube with moderate pressure. Then we installed the feed tube back into the ram, and after installing the new wear ring / guide band,  we reinstalled the ram back into the cylinder. Once completed the final step was to install the new oil seal and dust seal into the main gland nut.

New Oil & Dust Seals for Gland Nut

With new oil and dust seals in the gland nut, it’s time to install the nut back onto the cylinder, and it is a tight fit over the feed tube gland and ram. To keep from destroying the new seals, we placed a spacer on top of the gland nut and then used two bolts through two flat bars and threaded them into the top of the feed tube gland. This slowly pressed the gland nut onto the ram without damaging the seals. And that concludes the assembly of the cylinder.

Installing Gland Nut

Cylinder Assembled

Now, before reinstalling the cylinder onto the forklift, we needed to paint it. Jose uses a wire brush to strip all the old paint off. Then he masks off the chrome before applying primer.

Stripping the Old Paint

Applying Masking Tape

To conclude, I come in behind him with a new coat of gloss white industrial enamel. We then reinstall the cylinder in the same sequence used to remove it. The final step was to refill and bleed the hydraulic system and give the machine a good scrub and wash.

Applying a Coat of Industrial Enamel

Finished and Back in Service!

Everything worked out great bringing us to the conclusion of this project. My Allis-Chalmers ACP 80 is back to work and running great.

Until next time…

« Previous PageNext Page »

Create a free website or blog at WordPress.com.